The International Journal for the History of Engineering
& Technology
ISSN: 1758-1206 (Print) 1758-1214 (Online) Journal homepage: http://www.tandfonline.com/loi/yhet20
Restoring the Elsecar Newcomen Engine—High
Ideals, Deep Mysteries
Geoff Wallis
To cite this article: Geoff Wallis (2017) Restoring the Elsecar Newcomen Engine—High Ideals,
Deep Mysteries, The International Journal for the History of Engineering & Technology, 87:2,
154-164, DOI: 10.1080/17581206.2018.1462629
To link to this article: https://doi.org/10.1080/17581206.2018.1462629
Published online: 25 Jun 2018.
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INT. J. FOR THE HISTORY OF ENG. & TECH.,
Vol. 87 No. 2, July 2017, 154–164
Restoring the Elsecar Newcomen
Engine—High Ideals, Deep Mysteries
Geoff Wallis
Newcomen Society, London, UK
Elsecar is an important industrial area, once the powerhouse of the Fitzwilliam
dynasty of industrialists. Much of historic interest survives, including extensive
remains of its famous ironworks, mid nineteenth century workshops and the
unique Newcomen Beam Engine plus its mine-shaft. After decades of National
Coal Board (NCB) ownership and an uncertain future, the site was taken over in
1988 by Barnsley Metropolitan Council, who started an ambitious programme
of development at the Elsecar Heritage Centre. In 2009 focus turned to the
conservation of the engine and funding was obtained from the Heritage Lottery
Fund, English Heritage and the Council to carry out the work, that culminated
in an official opening in November 2014. Although much modified over its
working life, this engine is the only atmospheric beam engine in the world
that remains virtually complete on its original site and over its mine-shaft. It is
therefore of international importance, recognized by its Scheduled Monument
status. Conservation of the site required adoption of the highest standards.
This paper describes the extensive preliminary surveys, including under-water
investigation of the flooded mine-shaft, the ethical dilemmas of conservation,
and the challenges of interpreting a unique historic site for visitors, especially
the difficulty of providing access to a cramped three-storey industrial building.
The engine house and environs were restored and reinterpreted in 2009–2014.
On a project of international importance high ideals were adopted but some
deep mysteries remain.
Elsecar, Newcomen beam engine, Earl Fitzwilliam, Arthur Shaw,
cracked cylinder, A. K. Clayton, shaft
KEYWORDS
1. History
1.1. Construction and Working Life
A colliery was started at Elsecar Green by Richard Bingley in 1750 and taken over two
years later by the second Marquis of Rockingham. At this time the colliery had eight
© The Newcomen Society for the Study
of the History of Engineering & Technology 2018
DOI 10.1080/17581206.2018.1462629
RESTORING THE ELSECAR NEWCOMEN ENGINE
155
pits, and a horse-powered winding gin was used to bring up the coals from the Barnsley
Coal Seam around 50 ft from the surface. The 4th Earl Fitzwilliam inherited the estate
in 1782 and put in hand the development of both the ironworks and the colliery.
At Elsecar, the Barnsley ‘hard coal’ was available in a 9ft thick seam, ideal for making
coke for blast furnaces1 so a second colliery, the Elsecar New Colliery was developed
between 1794 and 95 to the north east of the Old Colliery, served by the Elsecar branch
of the Deurne & Dove Canal, which ran alongside the site. The canal greatly assisted
shipment of coal from the colliery.
The Steward of the Earl’s household records payments made for the shaft, engine and
house.2 At the start of shaft-excavation on 5th July 1794 a payment was made for ‘sod
ale, earnest for the sinkers, and ale for removing the gin and setting it up at the engine
pit’ A horse-gin was used for raising spoil and lowering materials in the shaft during
the excavation.
Payments were made to Michael Hague, Michael Hague Jnr. and Francis Hardy, mason.
Michael Hague, the Manager of Elsecar Colliery, lived in a house nearby. He supervised
a small team to sink the shaft. Hardy laid the brick lining, whose bricks were all wedgeshaped so as to form a ring that stays in place without any mortar. The shaft was dug
down whilst the bricks were built up in sections about three feet high. As each lift of
brickwork reached the section above it would have been difficult to insert the last brick,
so a slip-brick was used, held in place with an oak wedge, some of which can still be seen.
The brick lining extends down to 50 ft. below which the shaft was blasted out of
rock with gunpowder, dressed manually, and left unlined. At the bottom of the shaft
the sump from which the pump would draw was lined with bricks to protect against
erosion at an additional cost of £1 17s 8d. The shaft ran with water and conditions for
the labourers must have been both unpleasant and dangerous. They were issued with
flannel suits because of the wet conditions, and took five months to reach coal, a rate of
about 5ft excavated each week. Seven payments made to the shaft-sinking gang totalled
about £175. Around the same time a payment of £279 was made to a Sheffield supplier,
John Darwin & Co, for a ‘steam pan’ (wrought iron boiler) for the new engine, so the
boiler alone cost far more than sinking the shaft. The team appear to have provided good
value for the Earl, and records show that on completion in December 1794 payments
were made for a feast and ‘an entertainment for the Masons’. Their New Engine Shaft
remains intact after two centuries of use, neglect and continuous erosion by running
water, a tribute to their expertise.
The Engine House was constructed by the local mason Hardy using locally sourced
brick and stone. Records show that work started in October 1794 and was completed a
year later, not in 1787 as incised on the lintel over the door. The mystery of the origin
of this date is unsolved.
Responsibility for constructing the ‘fire engine’ was entrusted to John Bargh, an engineer living near Chesterfield. He obtained estimates for the components, certified them
on delivery, erected them, and probably commissioned the Engine himself helped by a
small team. Timber for the rocking beam was felled in the nearby Elsecar woods and
shaped for use during the autumn of 1794. The metal parts, weighing 16 ½ tonnes in
total, were supplied by Longden Chambers and Newton, John Darwin & Co. and the
Sheffield Park Ironworks for a total cost of £1,061 8s 11p.
156
GEOFF WALLIS
The ‘crab’ (manual winch) still extant on the bob gallery of the Engine house may be
the original used to erect the components, in which case it will be the oldest metalwork
on the site. Timber beams built into the walls at high level are suitably placed to hoist
the heaviest components. One beam still carries a pulley over which a rope or chain may
have run from the crab for hoisting light loads, perhaps the cast iron ‘junk ring’ which
secured packings to seal the steam cylinder.
The ‘Fire Engine’ was set to work pumping out the water in July or August 1795
allowing coal to be mined at greater depths in the dipping 9 foot thick Barnsley Seam.
Shortly after the pit was completed a ‘steam whimsey’ was installed for raising the coal.
Based on flow measurements recorded two years later A K Clayton calculated that
the Engine would have pumped for about ten hours per day if running continuously.3
Payments to one engine minder were made in September 1795, but by November a second
minder was being paid, so the Engine may have been working for longer hours.
1.2. Nineteenth Century
Bargh was called back in 1799 to repair the lower clack (valve) in the pump, which had
broken. Then in 1801 the Butterley Ironworks supplied a new 48 inch diameter cylinder
to replace the 42 inch cylinder, and the Coalbrookdale Company supplied three new
pumps to provide more pumping capacity.
By 1811 the original timber beam was in need of replacement having served for seventeen years. The new beam appears to have lasted for twenty-five years for Clayton in
his paper on the Engine4 records that in July 1836 Benjam Biram reported that the beam
was cracked and that the pumps were corroded and needed renewal. Messrs Graham of
Milton Ironworks quickly provided an estimate of £385 for a cast iron beam, parallel
motion, piston and 30 yards 9 inches of 21-inch cast iron pipes including a working barrel. These items are apparently referred to in the Wentworth Woodhouse Muniment as
the lengths of the pipes match the depth of the shaft, and the bore of the extant rising
is as stated in the estimate, so it seems likely that the major engine parts surviving on
site date from 1836.
The cast iron frame supporting the two valve arbors (horizontal shafts) is a mystery.
A Newcomen engine requires two arbors, one to operate the steam valve and a second
to control the injection-water valve. The extant frame carries bearings for a third arbor,
typical of Watt separate condenser engines, and its top transom is broken, so it is possible the frame was reused from another engine. Its origin and the date it was fitted are
unknown.
At some stage during the working life of the engine the cast iron pump stack, or rising
main, appears to have moved. One of the wrought iron pump-rods that hung from the
rocking beam had been cranked to an offset of about 6 inches to accommodate movement of the top end of the main, a feature that is shown on Clarence O Becker’s drawing
believed to date from the early 20th century. Timber clamps around the main wedging
against the stagings in the shaft were also added apparently to stabilize it.
The Engine continued to pump throughout the nineteenth century but no record of
its operation or maintenance have been found.
RESTORING THE ELSECAR NEWCOMEN ENGINE
157
1.3. Twentieth Century
Electric pumps were installed in the elliptic shaft to the south of the Engine (Ladder)
Shaft in 1923 and the Engine was retired from use. At this time, it was reported to be
running at 6 strokes per minute,5 less than half its original rate of pumping. However, it
worked again for about 6 months from January 1928 when the electric pumps failed. It
is probable that at this time the electrically powered Sirocco fan was installed to improve
up-cast ventilation in the shaft. The machinery still exists complete, but the fan itself is
unpainted and in poor condition.
The Newcomen Society visited Elsecar on 11th June 1931 and again on a summer tour
on 1950. In 1951 the Engine was steamed again for a Shell ‘Best in Modern Technology’
film series under the guidance of Sir Arthur Elton.
The NCB took over the Earl’s workshops in 1947 following the nationalisation of the
collieries. It was probably during this period that the timber pump rod was cut and a
steel frame with cast iron disc-weights was hung from the outdoor end of the beam to
counter-balance the weight of the steam piston. This would have caused the Engine to
rest ‘outdoors’ (with pump-rod end of the rocking beam down) allowing the Engine
to be operated by steam, but would not have provided sufficient resistance to withstand
the large forces generated by steam condensing the cylinder. The Engine could not therefore have been operated on steam safely, which may have contributed to an unexplained
incident.
1.4. The mystery of the Cracked Cylinder
In 1953 the NCB steamed the engine in preparation for a visit of the Newcomen Society,
although no record of a visit at that date has been found in the Society’s archive. At that
time Mr Arthur Shaw of the NCB Elsecar workshops was visiting the engine. It had been
started but would not run properly, apparently due to problems with the steam supply
and the water seal the top of the piston. The engine was stationary but Shaw describes
what happened next:
The engine came in once—with a heavy ‘bang’,—then a second time, even more noisily and
heavily, shaking plaster down,—finally a third time ‘with an almighty bang with plaster down,
bricks dislodged, plaster down, the building rocking and the sound of metallic fracture. The
engine then stopped’.6
This caused Mr Shaw and an apprentice in the house to ‘fly for their lives.’
It was assumed that the bottom of the cylinder was cracked on this occasion, but this
has been disputed by John Crompton and Jim Mitchell, who point out that the indoor
catch-wings arrest indoor movement some 500 mm before the piston strikes the false
bottom inside the cylinder that had been fitted before 1918 as it appears on a drawing
of that date. He asserts that the insert ‘was there to blank off the cracks in the cylinder
bottom and allow the engine to run without dismantling it to replace the bottom’.7
Consideration of what may have caused the engine to act on its own may, however,
lead to a different conclusion. During the recent restoration no damage to the insert nor
the underside of the piston were found, and measurements confirm that the piston could
not have impacted, so how could the damage have occurred?
158
GEOFF WALLIS
In early atmospheric engines the condensate drains from the cylinder via an eduction
pipe whose lower end is open, sited well below the cylinder and restricted to resist the
vacuum’s tendency to draw up water during the ‘indoor’ or ‘power’ stroke.8 In normal
circumstances therefore the engine is self-draining. At Elsecar the condensate passes via
a clack valve into a covered hot-well immediately below the cylinder, which is drained
by a pipe running outside the building. This pipe was cut, probably when the concrete
collar was constructed around the top of the shaft, and is likely to have been blocked.
Large quantities of water pass into the hot-well from steam condensing during warming or blowing through, from leakage of sealing water past the piston and possible leakage
through the injection water valve. In the absence of the original header tank, injection
water was probably provided by a water main at higher pressure than would have been
supplied by the header tank, causing leakage past the injection valve. Additionally, being
at rest with the piston at the top of its stroke, the injection water valve may have opened
allowing copious quantities of cold water to flood into the cylinder. Whether from leakage
or an open valve, the hot-well, overflow pipe, and the bottom of the cylinder filled to a
level at which any stroke would cause a hydraulic lock. If a vacuum then formed the piston
would strike the false bottom and the shock would be transmitted to the cylinder base.
The engine-man was outside the house at the time, so why might the engine have
moved on its own? Experience operating the full-scale replica Newcomen engine at the
Black Country Living Museum9 has demonstrated that an atmospheric engine will act
erratically if there is significant leakage around the piston allowing cold water to pass
the junk-ring packings into the steam space below.
At that time of the incident the engine was supplied with steam by the workshop’s
Lancashire boiler via the receiver still in place to the north of the engine-house. The
boiler is likely to have been operating at pressures far higher than the 1–2 p.s.i. required
by an atmospheric engine and even if fired sparingly it would have been difficult to restrict
the pressure to this level. The cylinder would therefore have become over-charged when
supplied with relatively high-pressure steam.
Steam would have vented around the piston, dislodged the packings and may have
allowed cool water to cascade into the cylinder condensing the steam. With very little
outdoor weight on the rocking beam the piston would have descended fast, impacting
the water. The steam valve may then have been opened by its linkages, or would have
remained open if warming through. A second charge of pressurised steam would then
replenish the space under the piston forcing it upwards, being condensed again by cool
water leaking past the piston, or injection water admitted by the valve that would have
opened at the top of the stroke, causing the second ‘indoor’ stroke.
Why would the third stroke be even more violent, as reported? By now more condensate
had collected in the bottom of the cylinder and more packing may have been shaken or
blown from the piston improving the drenching of the steam. It is also possible that the
pressure of incoming steam or shaking of the engine may have knocked the steam valve
closed which would have improved the vacuum but then stopped the engine after its final
indoor stroke. The cast iron insert is deeper on its front side so it is likely that the impact
would be greater on this side. This matches the configuration of the present crack that
runs around 70% of the circumference on the south side.
The conclusion should be drawn that the cylinder base was cracked in 1953 as reported,
not during its service life. This would explain why banding, the cheapest and most
RESTORING THE ELSECAR NEWCOMEN ENGINE
159
effective form of repair, was never carried out. It is therefore likely that the false bottom
was inserted in the nineteenth century during the widespread endeavours to improve the
efficiency of atmospheric engines, not as a means of sealing the cracks.
It seems that the decision was made at this time never to steam the Engine again, and
the Lancashire boiler was removed in 1954. It is perhaps not surprising that the event was
not officially recorded, and that new timber stops of considerable height, which survive
today, were fitted onto the indoor spring beams.
We owe a debt of gratitude to Arthur Shaw for recognizing the importance of this
story and for recording it in such clear detail. The accident demonstrates well the risks
of experimenting with an historic engine, and the value of working replicas.
1.5. Recent Decades
In June 1973 the engine was scheduled as an Ancient Monument and limited refurbishment, constrained by a lack of funding, was carried out by the NCB in 1981/2. This was
led by Mr Peter Clayton, NCB South Yorkshire Area Test Engineer, who recorded the
work in detail.10 Over twelve days valves, linkages and bearings generally were dismantled cleaned, lubricated and reassembled. Metal parts were cleaned and protected with
paint or anti-rust coating,11 two tons of debris, mostly ash and bricks, were excavated
from the basement, the cast iron junk-ring atop the piston lifted and wet, rotten spun
yarn packing removed.
The boiler feed pump was found to be badly corroded, buried in two feet of mud, its
shaft bent, and support beams broken, creating speculation that it may have been implicated in the 1953 accident. It was cleaned, painted and placed in the corner of the house
where it still stands. Reference is made in the notes to a ‘condenser pump’ with piston.
This is assumed to refer to the header tank supply pump in the pit which no longer has
its piston, a loss which has not been explained.
The engine was moved at this time, which bent the parallel motion bars because
the pump-rod bearings were seized. The author’s company Dorothea Restorations Ltd
straightened the rods in 1996–7 and reported that the rocking beam could then be moved
easily.12 The Company proposed a programme of repairs, painting and artificial activation
of the engine but this was not carried out.
The crack around the bottom of the cylinder was metal-stitched by Cast Metal Repairs
Limited of Wakefield in January 1984. Later that year the four-inch diameter lead injection water pipe, the bronze junk ring bolts and possibly other parts were stolen.
NCB engineers moved the beam annually by hand until 1987, but as collieries began
to close the demand for the workshop facilities declined leading to the closure of the
Elsecar facilities. Barnsley MBC purchased the Engine and workshops in 1988, the
latter subsequently being restored and opened to the public as the Elsecar Heritage
Centre.
The electric pumps were switched off in 1996 and removed the following year, although
their control gear was left in place in the pump house immediately to the west of the
Newcomen Engine House, where it still survives. Power to the site was disconnected in
1998 after which no work is known to have been carried out below ground other than
regular dipping to establish the water level in the shaft.
160
GEOFF WALLIS
2. The Shaft—a 100 Feet Deep Mystery
During the shaft’s service life an emergency escape route was created by stabilizing the
entrance to the Barnsley Seam with a concrete lining and construction of eight lifts of
steel-framed platforms and steel ladders with cast iron treads. Materials and construction
suggest that these may date from the early/mid twentieth century, perhaps constructed
at the same time as the 4 ft deep concrete collar that stabilizes the top of the shaft.13
At some time before the electric pumps were turned off in 1996 the windbore (the lowest
section of the rising main) and two clack-box doors were hauled to the surface, possibly
to reduce the weight of the pump-stack, or as an endeavour to retrieve as much historic
material as possible before the shaft was allowed to flood. No record of any shaft work
has been found in the NCB or Barnsley MBC archives.
The engine, house and shaft are all protected by Scheduled Monument legislation, but
the shaft had received little attention over the years having been flooded to within 8 m
of the surface since 1966, and, being a confined space below ground, was difficult and
potentially costly to access. The original brick lining and 22 inch (560 mm) diameter cast
iron rising-main were known to survive, but research yielded no archival information
about the structures below water. It was therefore imperative to investigate the shaft and
determine its conservation needs.
In 1993 the shaft was reported to be 45 m (148 feet) deep and flooded to 20 m (66 feet)
below the surface.14 The steel platforms were in poor condition and said to be supporting
the rising main by means of timber blocks described as ‘waterlogged and rotting in part’.
In a further inspection in 1997 Dorothea Restorations noted that the windbore had
been removed and that:
The rising main does not extend into the water of the sump, reflected daylight being visible at
the bottom of the bore.’ ‘It is possible to rock the head of the rising main to and fro from the
top landing indicating that it is not braced to, nor supported by any of the upper landings.15
It became clear that the historically important eighteenth-century shaft and its early
nineteenth century cast iron main had shown signs of distress in the past, and may need
to be stabilized. It was therefore imperative to find out whether the shaft was still open,
what it contained and its condition. In particular it would be important to know whether
the rising main was stable.
Initial investigations above water level revealed the top two ladders to be severely
rusted and have cracked cast iron treads. The top ladder was removed and stored in the
adjoining electric pump-house, the stagings cleansed, and the thickness of the rising-main
wall measured by drilling a small hole. It had lost a modest amount of probable original
section, but seemed otherwise structurally adequate. The brick lining, made of wedgeshaped bricks fitted without mortar, was generally intact, but bulged in two places.
The first underwater investigations were by side-scanning sonar lowered on a manual
winch from a scaffolding platform built over the shaft. This showed that the shaft was
open to the bottom, confirmed the depth, proved that the stagings and ladders were all in
place, and that the upper part of the rising main is leaning, confirming that it had moved
northwards about 9 inches (250 mm).16 Scanning the bore of the rising main showed it
to be filled with rust debris to a level below the lower clack box.
A visual inspection was then carried by a remotely operated vehicle (ROV) in crystal
clear water. Clearly visible were each platform and ladder, the heavily corroded cast iron
RESTORING THE ELSECAR NEWCOMEN ENGINE
161
main, the walls of the shaft, and the clack boxes from which the covers on the surface
had been taken.17 At Barnsley Seam level the concrete lined entrance was viewed but
was obstructed by a thin plastic pipe preventing the ROV from entering without risk of
its umbilical snagging. At this level a steel walkway fills much of the shaft, built around
the rising main which could be seen extending below. Repeated attempts to penetrate
gaps failed, and the ROV could not access the bottom of the shaft to view the structure
assumed to be supporting the main, none having been found at higher level.
Data provided by the sonar and ROV surveys enabled scale drawings to be prepared,
and provided enough certainty over the condition of the shaft’s structures to allow a
diving inspection. Access to the water was provided by a scaffolding suspended from the
surface, and controlled by a mobile dive-control station with continuous communication
between dive-master and the diver. Video monitoring of the operation from the surface
was achieved via the diver’s helmet camera. Working in good visibility the diver found
the pump-stack, stagings and ladders to be heavily corroded but apparently stable. The
plastic pipe obstruction at the entrance to the Barnsley Seam was removed and the diver
walked a short distance into the access passage proving that it was still open. A future
ROV inspection of the seam is thus possible.
A close inspection of the area where the rising main passed downwards through the
bottom staging revealed a possible access route into the bottom of the shaft, but this
proved to be obstructed by a strut and too dangerous to negotiate in full diving gear, so the
diver was withdrawn. It was decided instead to probe the depths from the staging using
a 2 m wooden rod with the helmet camera taped to its lower end. This revealed a solid,
regular surface, 1–2 metres below the staging, covered with a thin layer of lightweight
fine debris. The rising main could not be viewed closely but no structure of sufficient
size to support its estimated 20T weight was seen.18
Uncertainty therefore remains as to how the rising main is supported. It is known that
the lower half is leaning 250–300 mm but the upper section is vertical. It was stabilized
by pairs of timber blocks resting on stagings at four levels but that these are unlikely to
be carrying weight now. A hard, uniform surface exists just below the bottom (Barnsley
Seam) staging and no other support structure is visible. It has therefore been assumed that
the bottom of the shaft has been filled with concrete to support the rising main which
was known to be unstable. The windbore may have been removed to allow concrete to
be tipped into the rising main from the top, which would have been the easiest way of
carrying out the stabilization work.
Various options for stabilizing the rising main were considered, including ‘soft filling’
the shaft, which would be irreversible, or suspending the structure from the top, which
risked putting the castings into tension and cracking them if the shaft settled. It was
therefore decided that the best conservation option was to monitor the position of the
main to gather more information on its long-term stability and not attempt pre-emptive
stabilization until the need is proved.
3. Conservation of the Engine and House—High Ideals
The restoration project was overseen by a Partnership Board19 who decided at an early
stage that the site would be conserved as found with minimal alteration and modern
intrusions. Thus twentieth century alterations were retained, including steel pipe-work,
162
GEOFF WALLIS
some incomplete, and the feed-water pump was left in its relocated position. Missing
parts were not generally renewed, except for the injection water valve’s lead pipe and the
bolts securing the junk-ring to the piston as details were known and they helped visitors
to understand the engine.
Detailed surveys of the house, chimney base, engine, shaft and immediate environs
were carried out in 201120 from which contract documents were prepared and works
tendered competitively. Where photographs or other primary evidence showed structures
to have been replicated incorrectly in the past they were reinstated to an earlier appearance. Thus the head-frame that dated from the twentieth century was reconstructed to
an earlier design from photographs.
A determination not to replace steep ladders with new staircases in the house meant
that visitor numbers have to be restricted, and as the engine would move with visitors in
close proximity, parties would have to be supervised. However, guiding and restricting
visitor-numbers allowed a reduction in the level of guarding and lighting, and elimination
of interpretation panels from the house. Lighting was limited to dimmable LED’s above
stairs and walkways and new guards were installed around the rocking beam and over
the open cylinder only. The guards were specially-made detachable frames hooked or
clamped on to avoid drilled fixings and were laced with rope infill.
Electrical sockets for servicing each floor and their distribution cabinet were hidden in
cupboards, and behind a door. The risk of fire in such an important building justified a
modern detection system with extinguishers and a detector head which proved to be the
most visible of the few additions to the house. The survey of the engine revealed that the
piston, cylinder, pipe-work, valves and valve-gear were in relatively sound condition with
some historic wear and damage. Metallurgical tests on the metal stitches strengthening
the crack around the cylinder base proved the material to be mild steel, offering minimal
risk of galvanic corrosion.21
Severe decay in the two softwood beams supporting the rocking beam had caused one
bearing to subside 50 mm causing both parallel link-motions to twist and seize, possibly
bending their slender wrought iron rods. Dorothea Restorations jacked the subsided
trunnion-bearing back to its correct level and supported it on temporary timber blocks.
All bearings were dismantled, inspected, cleaned, greased and re-erected without renewal
and trials carried out in June 2013. The contractors were delighted to discover that simply
standing on one end of the beam caused it to stroke silently and smoothly, its first stroke
in more than two decades. The whole of the bob platform was subsequently renewed,
new beams being scarphed to sound ones inside the house.
Paint at numerous locations was analysed and its dozen strata found to be relatively
uniform.22 Metalwork was originally coated with several coats of black lead paint,
described as having the ‘appearance and texture of blacking or Zebo’. This had been
over-coated with red oxide (or possibly minimum orange), and grey or blue/grey. Later
coats are blue, then light green, overlaid by cream which was the finish coat at the time.
The joinery of the house carries a similar sequence, with more numerous later coats of
green. The antiquity of the historic coatings was uncertain, so it was decided that all
extant paint would be retained, regardless of its condition. The timberwork of the house
was re-painted green as found, and the engine coatings over-painted with single-pack
alkyd oil paint, sheen finish. The colour red oxide was chosen to match two earlier finish
coats, and new components such as guards were painted grey to distinguish them from
RESTORING THE ELSECAR NEWCOMEN ENGINE
163
the historic structure. Formerly polished metal-work was de-rusted and coated with two
applications of microcrystalline wax.
Impacts had cracked the indoor wrought iron catch-wing and the outdoor end of the
cast iron beam, which had been repaired by plating. The outdoor repair was dismantled,
cleaned, painted and reassembled, whilst the indoor catch-wing was load-tested to verify
that the cracked end would adequately support its own weight, avoiding the need for
an intrusive repair.
4. Animating the Engine
An important objective of the restoration project was to activate the Engine to enable
visitors to understand more easily the way it performed its role. A number of previous
reports had assessed the feasibility and risks of operating the engine, one suggesting
that it should be re-steamed. However, this was discounted at an early stage because
of the difficulty in providing a sufficiently large balancing load, the degree of intrusion
that would be required to restore or renew historic parts, conservation concerns over
introducing moisture to the inside of historic metal components, and the costs of capital
works, operation and maintenance.23
The brief adopted was that equipment to animate the engine would have to be automatic, capable of remote control by the guide, fail-safe and not put the historic components at risk in case of malfunction or derangement. New equipment would have
to be sited discreetly, not require any changes to be made to the historic fabric, and be
removable without trace. The least intrusive option was to place a small hydraulic ram
inside the empty cylinder of the water pump in the basement acting on the plug-rod.
This could only work safely retracting, drawing the indoor end of the rocking beam
downwards, so a replica pump-rod was constructed in steel to match the former timber
rod, and filled with lead shot to balance the beam heavy outdoors. One of the original
forked wrought-iron rods was reconnected so that it again entered the top if the rising
main from which it once pumped.
The hydraulic power unit was sited in the nearby electric pump-house to isolate its
noise and for ease of access. Its operation was controlled by a small programmable
logic circuit with proximity switches sited in the basement. The drive operates the
engine at half its original speed and mimics the action of operation under steam in
which the power or ‘indoor’ stroke is faster than the return stroke. In case of failure
the hydraulic equipment stops the engine and holds it secure until manually parked
and the system reset.24
The unveiling and opening of the newly restored site took place on 21st November
2014 with a spectacular light-show in which the engine house was bathed in coloured
light and its indoor moving parts projected onto the outside walls. A reception celebrated
the achievement was attended by many Newcomen Society members.
The Newcomen Society President Geoff Wallis and Vice President Michael Grace
met the Society’s patron HRH the Duke of Gloucester on March 11th 2014, acquainted
him with the restoration of the Elsecar Engine and presented to him copies of section
drawings of the engine and shaft. HRH Prince Edward subsequently visited the site to
view the restored engine, which is now open to the public and demonstrated regularly.
164
GEOFF WALLIS
Notes
1.
A. K. Clayton, ‘Newcomen Type Engine at Elsecar
West Riding’ (Read at the Institution of Mechanical
Engineers, May 1963 (1964).
2.
Fitzwilliam Wentworth Woodhouse Muniment,
Sheffield City Archives.
3.
A. K. Clayton, op cit., p. 103.
4.
A. K. Clayton, ‘Newcomen type engine at Elsecar west
riding,’ Transactions of the Newcomen Society, 35
(1962–3), 97.
5.
A. K. Clayton, op cit., Transactions of the Newcomen
Society p. 103.
6.
Barnsley MBC Archives a/81c/12/9.
7.
J. Mitchell, Elsecar Engine Report, Update, 2010, p. 131.
8.
L. T. C. Rolt and J. S. Allen, The Steam Engine of
Thomas Newcomen (Moorland Publishing, 1977),
Diagrams on pp. 37, 41.
9.
The Dudley replica engine was restored by the author
in 2011–12 and operates frequently.
10.
Barnsley MBC Archives, reproduced in Jim Mitchell,
Elsecar Engine Report 2010, Update, pp. 133–138.
11.
In a private conversation with the Author in September
2011 Peter Clayton stated that the coating was ‘black
rust inhibitor recommended by the navy’.
12.
Dorothea Restorations Ltd, (1997) Report The
Newcomen Engine at Elsecar, p. 13.
13.
Stabilization and construction of concrete head frames
at Hemingfield and Elsecar Collieries are reported to
have been carried out in the 1940’s.
14.
Museum of Science and Industry in Manchester
(January 1993), Report on the Restoration of the
Newcomen Engine at Elsecar, Barnsley. p. 6.
15.
Dorothea Restorations Ltd, op cit., pp. 18 & 19.
Atlantis Marine Ltd DVD held by Barnsley MBC
archives.
17.
Atlantis Marine Ltd, ROV Survey Report, 20–21st
September 2011, Barnsley MBC archives.
18.
Underwater Survey, Elsecar Mineshaft Video, DVD,
Commercial Diving & Marine Services. Barnsley MBC
archives. Dive carried out 28th March 2013.
19.
The Partnership Board comprised representatives
from English Heritage (now Historic England),
Barnsley Council, the Heritage Lottery Fund,
the project architect and engineer, and other
stakeholders. The author was appointed Engine
Consultant.
20.
The project was initiated in 2009 by Lynne Dunning,
Group Leader, Arts & Heritage, Barnsley MBC and
Dr John Tanner, Project Manager and subsequently
delivered by them.
21.
Caparo Laboratories, Willenhall, Laboratory Internal
memo, (2011), Barnsley Archives.
22.
Hirst Conservation Ltd, Results of Architectural Paint
Research to the Beam engine & Engine house, Elsecar
Heritage Centre, (November 2011).
23.
Dorothea Restorations Ltd, Elsecar Heritage Centre
Newcomen Engine & Shaft Conservation Study
(November 2011), p. 26.
24.
Restoration of the engine and provision of a new cover
to the shaft were undertaken by Lost Art Ltd of Wigan,
Lancashire.
16.
Notes on Contributor
Geoff Wallis is a Chartered Engineer, who trained as a mechanical engineer in the aerospace industry before taking up a career in conservation. He was managing director of
Dorothea Restorations Ltd for three decades specializing in repairs to historic metalwork
and machinery before becoming a consultant. Geoff is a long-standing Member of the
Newcomen Society and its Past President. He is a member of the Bristol Industrial
Archaeological Society and its current President. Geoff has contributed to a number of
books and journals and lectures widely on the conservation of historic metalwork and
machinery.
Correspondence to: Geoff Wallis. Email: jandgwallis@gmail.com